Thursday, February 27, 2025

Spring Gates

With the weather now getting warm, Uncle Lloyd and I decided to hang a couple gates. 


This is the northwest corner of the pasture. The 20' continuous fence panels ended about 6' before the corner post. So we decided to hang a saddle horse gate in its place. 


Springtime is prime time to burn grass. Better be ready to tend to fires if you're welding on the prairie. 


Good 270 degree turning radius. 


Should work. 


Next, was Grandpa's old white gate. This guy was originally hanging inside the barn. I think outside will do it well. 


To fit the gap we added a length of 2 7/8" to one side and welded it to the old hinge brackets. This also allowed us to have a way to mount the wood gate to the metal fence. 


Not being as tall as the other fence, we just split the difference from top to bottom. 


Simple mounting. Before we welded on the continuous fence panels, we dropped these pipe sleeves over the posts to serve as hinges. Then just welded a flat strap from one to the other. 


Giddy up.

Two down, six to go. Walk through gates are just as important as full-size grates. You want them functional, but also stylish. Think we checked both boxes. On to the next one. 

Sunday, February 23, 2025

Oil Pump

I'm not afraid to put a new engine in White Horse, whenever that day may come. But I'm also happy to tend to any repairs that can be done to keep this one running strong.


This original 6.0 V8 shows no signs of quitting. In 5,000 miles, she will burn about a quart of oil. Not enough to make me even think about an engine swap.


But you need good oil pressure. About two years ago she started running at about 30psi at idle. But when revved up a bit, she'd get back to 40psi. However, within the past few weeks, she has been hanging around 25psi all the time. And, until the oil got warm, she'd run dangerously low. So we set out to put in a new engine oil pump. 


Dave's shop in Gillette was our work space of choice. This is definitely a plan your work and work your plan kind of job. First thing was to make sure we had all the right tools. 


I'm a creeper guy. Ole Blue has served me well for the past 20+ years. 


Here's what we were after. Not a sump pump in the pan like I'm used to. This style runs off the front of the crankshaft.  


Chevy Vortec engines have actually been around since the 80s in V6s. In the mid 90s they started making the V8s with Vortec technology, and the power difference was noticeable! From my understanding, this feature of the Vortec has to do with good atomization of the fuel with the air in the combustion chamber. In the early 2000s they stopped making the standard Chevy small block and rolled into this newer LS V8. Tough engine. 
 

First step was to disassemble the front end; water pump and anything in the way of the timing chain cover. 


Getting the bolt out of the front end of the crankshaft was about as big of challenge as anything. Finally, this Milwaukee 1/2 impact did the trick. 


Then with a puller, we removed the harmonic balancer. 


That would be great if that was all the deeper we had to get. But because there is a siphon tube that goes from the pump to the bottom of the oil pan, we had to remove the oil pan too. Which, entails dropping the front differential. 


Some guys will wear protective gloves. But, I still prefer skinned knuckles. 


A good way to avoid whacking your hand, though, is by keeping an open palm when busting loose bolts. 


A few bolts and down she went. 


With that gone, we were able to expose the pan and drop her down. 


Then back up top to remove the timing chain cover and reveal the oil pump. 


This job was not for the faint of heart. Most bolts were barely in reach. 


Money.


I actually think this o-ring was the biggest part of the problem. It seals the suction line to the pump. I wasn't going to replace it until I felt how loose it sat in the pump. I bet it caused the pump to suck a lot air as it was trying to bring up oil. Especially when cold. 


Of course, we replaced the pump too. 


While we had the front end out, I wanted to replace the leaky axle seals as well. The drivers side you can just pop loose with this pickle fork tool. However, the passenger side you have to go in deeper. 


Here's an old farmer trick to give your end wrench a bit more leverage. 


After we disassembled the 4-wheel-drive engager, we were able to pull a clip, which allowed the axle to slide out. 


Then removed and replaced the seals. On these 1tons, everything is heavier. 


Then back in we put it. 


To top off the pumpkin with oil, just fill till it comes out the side plug. 


After we reassembled the front end of the motor, we filled her back up with fresh 5W-30. 


Muy bien.


The hardest part was the clean up. Where’s Dad when you need him. 


On the road again. 

Solid fix. The oil pressure jumps right up to 40psi at start up and stays there. I bet I can get another 100k out of this 6.0 with good oil pressure. Cheap fix for a big improvement. I'm glad we went through the effort. Could've had a shop do it, but where's the fun it that!? Special thanks to Dave for his shop and to Jared for keeping the trouble light out of my eyes. Ranch on. 

Golden Rule

Do unto others what you would have then do unto you.


Wednesday, February 19, 2025

Door Repair

The doors in the sacristy see quite a bit of swinging. Though they are 75 years old, they seem to be holding up good. Except for the one heading out into the sanctuary. 


I've been in and out of this door a hundred times and never thought twice about its integrity. Until I was visiting with Grandma on the phone and looking around at things I normally don't. Right in front of me was a crack clear through the door that run up and down the whole length. I'm surprised it didn't fall off right then and there! No sense in waiting until it does, though. Let's get it fixed. 


The basic plan was to screw it back together. The options of screws these days is amazing. When I can, I'm a torx man. 3 1/2" #10 screws with a 25 torx bit. 


If we split the difference of the screw right on the crack line, it should join the two halves back together nicely. 


The right depth is crucial. I only wanted to go about an inch in with the head before it started to tighten up. A piece of tape to mark where an inch is on the bit can work well. 


On a project like this, it is worth accurately spacing out the screws. This is good for both strength and aesthetics. 


Then screwed it up. Worked well. Because the door was still hanging on, it lined itself back up as the two halves were tightened together. We put in eight screws or so. 


Might as well finish the job right with a little wood filler. 


I just packed the holes deep and scraped off the excess with my pocket knife. 


Should work. 


Doors don't have much tolerances to spare. So, by tightening it up, we started to drag on the opposite top corner. 


A little 60 grit did the trick. 


Suck up the tailings. 


And we're back in business. 

What fun would life be if nothing ever broke down? Boring, for sure. I appreciate a good problem. Helps a guy grow in character. Through challenges, God can actualize a potential in us that we didn't know existed. My son, do not disdain the disciplines of the Lord! (Proverbs 3:11) Let's ranch. 

Poverty

Is a total dependance on God.             https://youtu.be/UX49gXXth7w